It has been project after project time, as our date to sell the car and move the boat draws near.
We expect a certain amount of delay for each project, waiting on parts - sometimes ordering wrong part and having to re-order, unexpected issues and so on.
There are other projects, that just beat you down.
We have been working on installing our new VHF antenna, our new cell phone booster, our new Wifi antenna, and our new GPS antenna. All these go on our big aluminum arch on the back of the boat, and then the wires are fed through the aluminum tubes, down into the boat, under the bed, behind the guest stateroom storage drawers, and then up into the cabinet behind the TV into the respective control units mounted with power. It is a time consuming project, but has been going well. A couple of wrong fittings, fed one wire wrong and had to re-do, but all in all going well.
A little bit of contortionism to get things hooked up, but all in all, progressing nicely.A couple of other projects have been a little more difficult.
Our hot water heater had a leak - a constant drip.Wasn't surprising, as it was quite corroded.
Not bad when hooked up to dock water, but when you have limited water at anchor, - no drips allowed. Our water heater has a special flow thru pressure relief valve - so that was a special order - no issues, but after that it went downhill quickly. No mater how much teflon tape, plumbers putty, or locktite, it leaked around the new fitting.
The previous owner had changed them as he wanted gauges at the helm for oil pressure, water temp, voltage and engine hours - unfortunately no RPM, which is what we really wanted at the helm.
Control panels as we wanted. |
After it was all wired up, the moment of truth - try to start the engine. First try - nothing. So out came the multimeter, and a miriad of checking voltage and continuity. Found that the hidden side of the lovely 16 pin connector had corroded so badly, that one pin was missing, and a couple halfway gone. So back to Amazon, and ordered some new connectors. Pause 4 days, and once they came in, we set about re-wiring and installing a new connector. Once all was done, then 2nd try to start engine - Nothing. So out came again the multimeter, accompanied by much hair pulling by Kris. It was late, so Dean called a halt to the day. Next morning with fresh eyes, Kris quickly found the issue with a loose connection (not one we had done) and fixed that.
We took the starter in, got it checked, and sure enough it is bad. New starter comes later this week. Will have to let you know how it goes -but if it doesn't go well - Kris may call it - and we might have to hire someone to help fix this one, as she is about at her limit of knowledge on how to fix the issues.
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